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Tertiary oil recovery by CO/sub 2/ injection. Quarterly report, April--June 1978

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Total water injection for the quarter was 17,370, an increase of approximately 2700 barrels over the previous period. The increase was due to remedial work on the input wells that was completed during March. The only problems occurred during June, when excessive shutdowns resulted from line plugging after moving the water tanks. This problem was subsequently solved. Oil production for the period was 4314 barrels, an increase of approximately 660 barrels over the previous quarter. Although increases in production were experienced in wells outside the pattern, the central producer continued at about 1 barrel per day with increasing water production. Total production attributable to CO/sub 2/ injection is 8562 barrels.

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Last Updated September 29, 2016, 16:11 (LMT)
Created September 29, 2016, 16:11 (LMT)
Citation Conner, W.D. ---- Roy Long, Tertiary oil recovery by CO/sub 2/ injection. Quarterly report, April--June 1978, 2016-09-29, https://edx.netl.doe.gov/dataset/tertiary-oil-recovery-by-co-sub-2-injection-quarterly-report-april-june-1978
Netl Product yes
Poc Email Roy.long@netl.doe.gov
Point Of Contact Roy Long
Program Or Project KMD
Publication Date 1978-9-1